Author Topic: Repost: power loss issue  (Read 68669 times)

Offline 1979C20

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Re: 700R4 issues...
« Reply #45 on: December 15, 2010, 10:22:52 pm »
Vile, about my friends jeep, what is the modulator? Like I said, don't know much about trans.
1979 SCLB C20 Q-jet 350 SM465 14b F.F. 4.10 G80
1989 GMC Suburban V2500 TBI350 TH400 4in lift 35's 14b SF

Offline VileZambonie

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Re: 700R4 issues...
« Reply #46 on: December 16, 2010, 02:50:29 pm »
Can you find out what trans he has? I don't want to hijack this thread so make a post about it in General Discussion but the vacuum modulator delays upshifts and helps with downshifts in response to engine load. It gets it's signal from a manifold vacuum source.
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Offline 1979C20

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Re: 700R4 issues...
« Reply #47 on: December 16, 2010, 04:36:02 pm »
Okay vile. Ill find out what trans it is and post it in general. Sorry for post stealing! Ha. Thanks guys. Good luck with your trans/engine issues.
1979 SCLB C20 Q-jet 350 SM465 14b F.F. 4.10 G80
1989 GMC Suburban V2500 TBI350 TH400 4in lift 35's 14b SF

Offline nativetexan

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Re: 700R4 issues...
« Reply #48 on: December 21, 2010, 07:33:17 pm »
Got a trouble code 44 today. I havent checked the fuel pressure yet. i am waiting for it to come back to my autozone down the street. I checked the code definition online and it said O2 sensor-too lean. Your thoughts? I will check pressure tomorrow.

Offline VileZambonie

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Re: 700R4 issues...
« Reply #49 on: December 21, 2010, 08:06:40 pm »
Low fuel pressure/ large vacuum leak
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Offline nativetexan

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Re: 700R4 issues...
« Reply #50 on: December 22, 2010, 11:39:12 am »

something strange (i noticed), I double checked my vaccuum lines and I didn't have my EGR solenoid connected. I connected it and it seems to have made it worse.

Offline nativetexan

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Re: 700R4 issues...
« Reply #51 on: December 22, 2010, 12:30:30 pm »
Also, it blows my mind that it runs awesome everytime I disconnect the fuel line. I took the back side of the filter off so I could see what it looks like when I turn the pump on. A little bit more than a dribble.  >:( But the wierd thing is when I connect it back, it runs like a champ! I wonder why...

But yeah, I am dealing with a low pressure issue. Should I replace the pump or should I do some more checking?

Offline nativetexan

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Re: 700R4 issues...
« Reply #52 on: December 25, 2010, 06:45:57 am »
Bump... please. ;D

Offline VileZambonie

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Re: 700R4 issues...
« Reply #53 on: December 25, 2010, 07:36:00 am »
Your EGR solenoid was probably disconnected because it's most likely stuck open making it open the EGR valve = run like poop.

Replace your fuel pump
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74 GMC, 75 K5, 84 GMC, 85 K20, 86 k20, 79 K10

Offline nativetexan

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Re: 700R4 issues...
« Reply #54 on: December 25, 2010, 08:39:43 am »
Thanks man! Should I replace the solenoid too??  :-\

 :o ;D  MERRY CHRISTMAS!!!    ;D  :o

Offline VileZambonie

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Re: 700R4 issues...
« Reply #55 on: December 25, 2010, 08:42:38 am »
Not until you test it.
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Offline nativetexan

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Re: 700R4 issues...
« Reply #56 on: December 25, 2010, 08:49:29 am »
RIGHT!

Offline nativetexan

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Repost: power loss issue
« Reply #57 on: June 22, 2011, 03:52:52 am »
So, I am still having a power loss issue. I know it has something to do with the fuel pressure cuz I put a pressure guage on the line and am losing pressure when I rev it. Dropped the tank, replaced the pump motor, but not the assembly. Still the same no improvement.

Any Ideas?

Offline Irish_Alley

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Re: Repost: power loss issue
« Reply #58 on: June 22, 2011, 04:09:15 am »
the only post i seen is about the tv cable? is there another one or is that it. refresh our memory about your problem. go ahead were listening
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Offline nativetexan

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Re: Repost: power loss issue
« Reply #59 on: June 23, 2011, 12:10:26 am »
When I rev my pedal, it goes and then it bogs like its not getting fuel. When I drive it does the same thing. If I try to get on it, it just bogs out like it has no power. The last advice I got was that it was the fuel pump, so I replaced the motor not the whole assembly. I have plugged up all the ports on the TBI that I am not using (Smog stuff). I tried running chemtool through it to see if the lines were clogged. The only time I have gotten rid of it was when I took the filter out to replace it thinking the filter was clogged. But it only lasts for the first drive. After I shut it off, it does it again. its a remanufactured 350 that I put in myself with the original TBI on it. I tried not to frankenstein it too much. The only thing I question is the lack of the smog equipment on there with all the vacum ports plugged on the throttle body. And thats pretty much it.